TY - GEN
T1 - Effects of purge jet momentum on sealing effectiveness
AU - Clark, Kenneth
AU - Barringer, Michael
AU - Thole, Karen
AU - Clum, Carey
AU - Hiester, Paul
AU - Memory, Curtis
AU - Robak, Christopher
N1 - Publisher Copyright:
Copyright © 2016 by ASME.
PY - 2016
Y1 - 2016
N2 - Driven by the need for higher cycle efficiencies, overall pressure ratios for gas turbine engines continue to be pushed higher thereby resulting in increasing gas temperatures. Secondary air, bled from the compressor, is used to cool turbine components and seal the cavities between stages from the hot main gas path. This paper compares a range of purge flows and two different purge hole configurations for introducing the purge flow into the rim cavities. In addition, the mate face gap leakage between vanes is investigated. For this particular study, stationary vanes at engine relevant Mach and Reynolds numbers were used with a static rim seal and rim cavity to remove rotational effects and isolate gas path effects. Sealing effectiveness measurements, deduced from the use of CO2 as a flow tracer, indicate that the effectiveness levels on the stator and rotor side of the cavity depend on the mass and momentum flux ratios of the purge jets relative to the swirl velocity. For a given purge flow rate, fewer purge holes resulted in better sealing than the case with a larger number of holes.
AB - Driven by the need for higher cycle efficiencies, overall pressure ratios for gas turbine engines continue to be pushed higher thereby resulting in increasing gas temperatures. Secondary air, bled from the compressor, is used to cool turbine components and seal the cavities between stages from the hot main gas path. This paper compares a range of purge flows and two different purge hole configurations for introducing the purge flow into the rim cavities. In addition, the mate face gap leakage between vanes is investigated. For this particular study, stationary vanes at engine relevant Mach and Reynolds numbers were used with a static rim seal and rim cavity to remove rotational effects and isolate gas path effects. Sealing effectiveness measurements, deduced from the use of CO2 as a flow tracer, indicate that the effectiveness levels on the stator and rotor side of the cavity depend on the mass and momentum flux ratios of the purge jets relative to the swirl velocity. For a given purge flow rate, fewer purge holes resulted in better sealing than the case with a larger number of holes.
UR - https://www.scopus.com/pages/publications/85210058927
UR - https://www.scopus.com/pages/publications/85210058927#tab=citedBy
U2 - 10.1115/GT2016-58099
DO - 10.1115/GT2016-58099
M3 - Conference contribution
AN - SCOPUS:85210058927
T3 - Proceedings of the ASME Turbo Expo
BT - Heat Transfer
PB - American Society of Mechanical Engineers (ASME)
T2 - ASME Turbo Expo 2016: Turbomachinery Technical Conference and Exposition, GT 2016
Y2 - 13 June 2016 through 17 June 2016
ER -